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Donnie's JAPAN ADVENTURES Thread

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  • BigGameHit
    replied
    roger that im back on sort of a normal schedule again.. I also made Staff Sergent in the Air Force so extra money. good timing lol

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  • INFO
    replied
    thanks for the update Donnie,

    got you back on the homepage

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  • BigGameHit
    replied
    The day started wet but quickly dried. This was shake down day to see if my setup was good enough to slide. The day started out shitty because the car was pretty much driving itself. With the help of a buddy, I noticed that my Throttle Body (TB) was still sticking mechanically and it was not a PFC (Power FC) issue. After taking the TB apart at the track, I notice that a bit of RTV forced its way around the opening of the TB mouth causing the TB plate was getting caught on it delaying the release. After fixing that issue.. the car was splendid. I was super happy with the response of the turbo and my tuning ability. The air/fuel ratio's were on point and I can actually increase timing in certain areas as my knock was minimum.

    This was my first time sliding since March 6 2010 due to the fight on terror. after about a few laps and getting use to the new setup things were normal. Toward the end of the day, half track opened up into full track. At that point I set my eyes on doing the wall all the way down. Half track I can do all day... however I am currently 0 for 2 on attempts at full track wall sliding. I can't believe I cleared Ebisu circuits jump/wall and screwed up here lol..... part of the game. Ill re-grope and come back stronger. Looks like im going to miss D1SL which is tomorrow and MSC on June 5th.. unless the guy sells me his car quickly.

    As you will see from the video, I broke through the wall, at that point I could have stopped drifting.. I tried to use the momentum of the wall to set up for the rest of the straight away sadly my tires didn't not respond....... it seemed cool in my mind.. but didn't work out that way as I went right for the tractor tire and dirt hill that was luckily very moist from rain. On lookers say that I hit the tractor tire knocking it out of the ground with my driver side, did a 180deg spin in the air 1 foot above the hill and land on it. I was calm the hold time and I knew this car was done on impact as I was in 3rd gear approaching the wall. My engine was still running strong on top of the hill.. and I had zero leaks so I was happy with that portion.

    One of the spectators that came with me drove an N/A 5speed R33 (black with burgundy front bumper in video). I asked him straight out 10 min after the wreck "how much" he replied $1300, I said "sold" and we shook hands. The transaction will go down this week.

    Now I gotta look at the FSM's and see whats really different electrical wise from the NA RB to the Turbo RB.. much of which don't apply because I'm not using any of the stock electricals besides the vitals.

    I highly recommend putting a cage in your drift car. I know most do but some don't. This bolt in cage that I spent 250 dollars on saved my right foot from being broken or damaged. The sidewall of the car is against the gas pedal and was stopped by the front right leg of the bolt-in cage.

    pictures and video...


















































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  • BigGameHit
    replied
    ...........more to come

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  • blu808
    replied
    I'm painting my fuel rail pink.

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  • BigGameHit
    replied
    Current Engine bay setup

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  • BigGameHit
    replied
    manifold fixed.. now just trying to tuning the car... sorta hard as im in a military college course at the time which is very demanding. after the class is done.. Ill be able to really dive into the tuning.

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  • BigGameHit
    replied
    little valve cover play, converting to Low impedance injectors and deleting much of the stock coolant lines.








    Car currently is idling at 2000 rpms I have not beee able to really diagnose as work has gotten busy again. The air intake control valve is all good to go and all vac sources are plugged or used. Ill have to check and set the voltages of the TPS that should do it for sure. Also had an unfortunate yet cool event take place....... I have a hair line fracture on the pictured part of my manifold. Coolant is leaking out through a crack.. going to have to get this welded by a welder thats set up for Aluminum :/. The location could not have been better... right up front.

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  • BigGameHit
    replied
    Status as of three days ago........





    the "completion" of this build was made possible by Ryan for letting me borrow his RB powered Z31... I love driving this thing.




    Work on the exhaust housing dumptube took some time do to the crazy angle and having to make multiple passes on the welds and grinding them down in between each session. When I started the the car there were only a few pin hole leaks which I welded up.






    Last edited by BigGameHit; 10-22-2015, 02:39 AM.

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  • BigGameHit
    replied
    http://www.youtube.com/watch?v=EV_6TBSGCE8

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  • BigGameHit
    replied
    well I forgot I had to return to work... its 338 right now... Had to call it a night. Car should start tomorrow for sure.. All I need is some fresh fuel line... *Censored**Censored**Censored**Censored* reusing the old hard rubber lines I had.

    the intake manifold is cool.. but *Censored**Censored**Censored**Censored* man... it was a *Censored**Censored**Censored**Censored**Censored* putting the bolts in... such tight clearances.

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  • BigGameHit
    replied
    sadly nothing... i have to go fight terror soon... just got notified... everything is canceled. it was both

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  • Bebop
    replied
    Getting ready for MSC or D1SL?

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  • BigGameHit
    replied


    Got down to business finally on the turbo setup. Day 1 started at 1600 on Sunday and terminated 10am Monday.... My fingers hurt badly but Ill be going back out to work untill complete exhaustion again lol.




    Had to bring the temp of the cast housing up in order to change the properties of the metal so that I could weld on my stainless steel Vband flange.







    Don't wanna mess up the clean for so soon..



    My new little paint box lol... didn't want to paint inside the garage today.





    Bye Bye Stock... its been a good run but its Ova!



    Was shocked that the RB T28 turbo has a T3 exhaust housing flange. Gee Wiz info. Had this been a smaller holset... I could have bolted it right up to the cast manifold if I wanted. This also made running my oil return super easy as I was able to use the T3 return fitting from the T28...(Peter Griffin) "Yeeaaaaaaaa"



    Had some unforseen fitment issues due to my manifold.. If I had more time on my hands.. I would have just sources a new manifold.. but that's not an option.. so whats a Ninja do????......grinds away safely untill it fits.... This process took about 2-3 hours alone do to removing and installing every time will all gaskets to insure the fitment is good to go.

    I can't fab up the dump until I install my new motor mounts... which requires some modification themselves. Gotta do some research and see how RB's do with atmospheric WG setups..... for Japanese Inspection purposes I think im just going to run the WG into the dump.











    AC is no more.. never used that *Censored**Censored**Censored**Censored* as Misawa is Cold 295 days a year. the AC was pissing me off due to how I would have had to route my dump... I Could have bent the hardline...but all that jazz is gone bay is so much cleaner all ready.



    Wrapping it up for that session.

    Fitment is tight.. but it works. will sand and paint the covers. Next is to see what All I can get rid of in the coolant sections.







    Tonights objectives..

    -Install new mounts
    -mock up dump tube
    -install intake manifold
    -wire up resistor pack for bigger injectors
    -we shall see

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  • BigGameHit
    replied
    Im Back online!!!!!

    much has happen since my last time online from home.... here its all is....

    Late March

    Moved into my house. garage is a little tight but its ok. I keep all of my tires and spare parts in my storage sheds. don't want to clutter the place.













    Prepping the turbo and painting some new drift wheels up while I wait on last minute parts over night from USA!!!!!









    PhotoShoot....











    Little cappuccino.. so cute.. I want to drift one



    April

    Was trying to sell these Work's but the offset are not that great.. I decided to keep them.... I done like silver wheels much so................














    Took a break and went to go help out some other Gaijins..





    Finished

    Last edited by BigGameHit; 04-12-2010, 02:08 AM.

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